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Pellet Stove Exhaust Blower Motor fix update

November 27, 2010 Leave a comment

I’ve updated one of my older posts (ok really old) on a noisy exhaust blower motor on a Whitfield Advantage Optima 3 FS pellet stove (now owned by Lennox Hearth Products).  The update was largely due to my annual deep cleaning of my in-law’s stove and learning things along the way.

If you are into this kind of renegade after market noise reduction solution, go check it out here:

https://dompruitt.com/2008/12/25/whitfield-advantage-ii-pellet-stove-noisyrattling-blower/

– Dom

Whitfield Advantage Optima 3 Pellet Stove – Noisy/Rattling Blower

December 25, 2008 2 comments

Ok, here’s a quick fix to a Whitfield Advantage Optima 3 noisy or rattling exhaust motor.

I found the rubber bushings that supported the full weight of the exhaust motor was not sufficient.  This resulted in vibration when the motor was running (it runs all the time since it’s a exhaust motor that vents combustion gases).

My In-Law’s Pellet Stove (I bought it for them):

All I did was brace the exhaust motor with some simple things you can find at a local hardware store.  The parts I used was a band clamp, galvanized strapping (used when building a house or patio), a metal screw, and a washer.  All the parts are metal since this motor gets quite hot.

Here are the pictures to show what I did (the exhaust motor is on the left side of the stove):

This is the exhaust motor with band clamp and galvanized support clamped on.

 

Just a close up to show some clearance between band clamp & motor wires, also see the motor support.

 

This photo shows how the galvanized strapping was bent to loop through the band clamp & create feet to screw to the bottom.

 

Sheet metal screw & washer to hold the base of the new motor support.

 

Hope this is useful to others.

– Dom

HVAC "service professional" experience

November 10, 2008 3 comments

Ok, here is my account of a recent bad experience with a local HVAC / Climate Control company and how I did some additional research and troubleshooting to replace a White-Rodgers control board on the York Diamond 80 Furnace/AC unit in my house to save about $300.

*** START DISCLAIMER ***

Of course, it goes without saying for things of this nature … if you are NOT TECHNICALLY INCLINED/COMPETENT (or have the right tools) to do this yourself, please employ a professional since the risks are high to you personally and/or your home.

*** END DISCLAIMER ***

The initial problem started when we tried to start the heater for the first time this season. The furnace was not blowing hot air to heat the house. It was blowing cold air.

Here it the HVAC unit in my house:

I checked the control board and it was flashing some lights indicating something was wrong (error codes). The LED is on the lower left of this picture in red.

The flashing code sheet on the control unit indicated the pressure switch was stuck closed.

Here is the upper (heat) portion of the HVAC system:

The pressure vacuum switch is just by the exhaust blower motor, and it connected to it by a clear vacuum hose (upper part of the picture). I checked the switch with a meter (continuity test) and put some vacuum on it and it open and closed properly, so this was not the problem.

Since this all happened on the weekend (Saturday) and I was leaving town on Tuesday and it was starting to get cold here, I called a local HVAC company to fix this for me. I did not want my wife and kids dealing with a cold house (and a service person) while I was out of town for the rest of the week.

I found one of the HVAC service companies working on the weekend, so I asked for a service technician to come over to fix the unit.

The guy arrived and started to check things out, I watched intently so I could learn something since this was running me about $80 just for the visit.

He saw the same flashing error code, then checked the switch, then checked the voltage going to the exhaust blower. Went through several startup sequences. After all that he said the problem is likely a bad control board or a bad exhaust blower.

I asked if there was a test he could perform to just test the exhaust blower to rule it out as a problem. He said it was highly unlikely that the exhaust blower was bad, more likely the control board. I found it quite frustrating that I was paying him to diagnose the exact problem only to get this answer. All I was looking for was a simple test to make sure the exhaust blower was working.

He got on his portable laptop to lookup the replacement control board for this unit to fix it, and he was unable to find the exact replacement. He said the company can call on Monday for a quote to fix it. He swiped my credit card, charged $80 for the visit and left.

He really did not help my situation, but I learned something from the visit. As much as you think these folks know what they are doing, they still fail to satify the customer/me (by ruling out the exhaust blower as the problem).

He also missed a significant problem. I found the large blower (main air mover to the house) had charring on the capacitor terminals with some melted leads (due to someone cinching down the cable tie too much at some point in the past). Since the blower was working, I assumed the capacitor was still good, so I cleaned up the connections and replaced the terminators as shown below.

Still without heat, I went to work testing the exhaust blower. Since it was a 60 Hz 110 AC motor, I found a old small appliance plug, cut it, striped the leads, and connected it to the motor connectors to briefly see if the motor would turn (I would like to point out that I know about testing this safely and want to point to the disclaimer for your situation). After some work, the motor turned and that was not the problem. I went online to see about finding a control board.

The control board I had was a White-Rodgers 50A50-241, I went to www.white-rodgers.com to find more info about this board. It was an old board, and it was replaced by a 50A55-843 control board. Searching around, I found it as much as $100 and as high as $250 on the internet. Since I needed this board fairly quickly, I called some local service & repair places to find it locally. Not many of these people are open on the weekend, so I had to wait until Monday.

Monday morning, the HVAC company called, it would cost $500+ to fix the unit, and it would require a “part acquisition fee” since the part was in a nearby large city (is this a new way of getting more $ out of you?). This did not work for me since I was leaving town the next day. The internet did not work also, since the part would take a day minimum to get here.

Meanwhile, I did find the control board at local plumbing/heating/cooling retailer, it was $200. I drove to the retailer to pickup the board and went home to install it before leaving town the next day.

I can say, the newer control board has plenty of information on the website, such as a troubleshooting document that would have been very helpful with the older one I was having trouble with.

I took pictures of all the connections of the old board, labeled all the connections also. Then drilled two new holes to mount the new control board since it was smaller than the old one (used 2 of the old holes to mount the new board).

All the connections were the same if not very similar, so pretty easy to replace a old board with a new one. Here is what it looked like after installing it (remember to disconnect the power before doing anything electrical).

Thinking back to this summer, there was a lightning strike very near to the house that took out a printer (connected to the phone line) & a cordless phone. Maybe it had something to do with the heater part of the control board, who knows?

All in all, I managed to provide my family with heat at a cost less than a “service professional”. I was rather fortunate that a local retailer had the control board for a reasonable price under the time constraints I had.

I hope this post helps some folks out there with my experience.

Take care & be safe.

– Dom

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